Outdrive1
Outdrive1 Marine Sales https://www.outdrive1.com/
- Joined
- Dec 19, 2007
- Messages
- 33,539
- Reaction score
- 30,743
So I'm freshening a 620cu Aluminum BBC.
This motor had 20 hours on it when I got it. The Magnaflow cam driven water pump leaked into the motor. I had water in the oil and couldn't find the cause. Pulled the headers. Tested them. Then pulled the intake. Looked for leaks. Then pulled the heads looking for a bad head gasket. Pressure checked the heads. Still couldn't find an issue. So out came the motor. Wasn't until I tore it down that I discovered the pump leaking.
I figured why I have it all apart. I might as well do all new bearings and rings.
Motor is an all aluminum Keith Black KB600. Basically it's a 1" tall deck. It's also 18 degrees. Dart Big Chief Pontiac Heads. Dry Sumped. Keith Black Knife Edged Crank. 4.75 stroke. 4.520 bore. 13/1 compression on race gas.
I got Barry involved once I started digging into it. I just wanted it back to stock and fresh. The old Felpro Head gaskets were 90's technology.
By the time I had the cylinders honed we realized that it was going to end up 4.540 bore. So I figured I might as well drop the compression to 11.5 so I could run AV gas instead.
Next call was to Jeremy at RaceTech. Barry gave him a deck height and they came up with some custom pistons. With in a day Jeremy had a cad file, and a couple of days later like magic a custom set of pistons. I'm still amazed how fast he pulled this all off.
This motor had 20 hours on it when I got it. The Magnaflow cam driven water pump leaked into the motor. I had water in the oil and couldn't find the cause. Pulled the headers. Tested them. Then pulled the intake. Looked for leaks. Then pulled the heads looking for a bad head gasket. Pressure checked the heads. Still couldn't find an issue. So out came the motor. Wasn't until I tore it down that I discovered the pump leaking.
I figured why I have it all apart. I might as well do all new bearings and rings.
Motor is an all aluminum Keith Black KB600. Basically it's a 1" tall deck. It's also 18 degrees. Dart Big Chief Pontiac Heads. Dry Sumped. Keith Black Knife Edged Crank. 4.75 stroke. 4.520 bore. 13/1 compression on race gas.
I got Barry involved once I started digging into it. I just wanted it back to stock and fresh. The old Felpro Head gaskets were 90's technology.
By the time I had the cylinders honed we realized that it was going to end up 4.540 bore. So I figured I might as well drop the compression to 11.5 so I could run AV gas instead.
Next call was to Jeremy at RaceTech. Barry gave him a deck height and they came up with some custom pistons. With in a day Jeremy had a cad file, and a couple of days later like magic a custom set of pistons. I'm still amazed how fast he pulled this all off.